IRS/2025/7012/OCR
Notification details
| Status | Completed |
|---|---|
| First observed date | 26 November 2025 |
| First observed time | 15:30 |
| Organisation involved | BP EXPLORATION OPERATING COMPANY LIMITED |
| Installation | Andrew Platform |
| Field | ANDREW |
| Latitude | 58° 2' 51.122'' N |
| Longitude | 1° 24' 15.552'' E |
| Quadrant / block no. | 16 / 28 |
Breach details
| Related to a breach where an OCR permit is in place | Yes |
|---|---|
| Breached conditions | Condition 2 Permitted chemicals. OPRED PON1 Guidance Appendix E: 'Non-compliant discharges from subsea hydraulic control system include: • control valves seized or stuck in position that results in an emission of hydraulic fluid from the location intended to discharge hydraulic fluid' |
| Related either wholly or partially to use and/or discharge of a chemical(s) | Yes |
Chemical 1
| Chemical product released | Castrol Transaqua HT2 |
|---|---|
| Total quantity of chemical used in excess of permitted quantity (kg) | 0 |
| Total quantity of chemical released in excess of permitted quantity (kg) | 610 |
| Related to a subsea discharge | No |
|---|---|
| Was the subsea discharge greater than 1 tonne over 12 hours | No |
| Was the non compliance ever ongoing | No |
Formal investigation
| Formal investigation ever opened | No |
|---|